MOS Slit Cutting Test-2 Japanese
Tokoku
10/10/2006 Updated

Past Test (Japanese), 6/2004

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Test Objective
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Omata-san's suggestion :
>>>1. Cutting speed improvement with laser cutter.
   2. New high power laser cutter.
   3. Using EDM.
   4. Photochemical etching.
(This report is about 1.)

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Test procedure 
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>>>( 1 ) Find best parameters.
   ( 2 ) Make many slits with different widths at different position.
   ( 3 ) Measure the slit widths with microscope and
         determine relation between inputs versus outputs of the laser.
   ( 4 ) Cooling test with CIAO test dewar if anodized mask will be used.
   ( 5 ) Cooling test in MOIRCS with stars and pinhole-mask
         if anodized mask will be used. 

   ( - ) Ask for Yutani-san for cutting anodized material with laser.
         ( Exhaust instrument might be different. )

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Tests & Results
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Result
5: Perfect cut ( cutoffs drop off )
4: Acceptably cut ( cutoffs drop off by giving a gentle nudge )
3: Almost cut ( there are some cutoffs left )  
2: Occasionally cut ( hard to drop cutoffs off )
1: Almost never cut

w/MOIRCS frame, 1-time cutting for each slit     ... Test w/FOCAS frame

Aluminum Type Current Frequency Marking Speed Cutting
Feed Rate
Result Comment
Hard-temper
(alloy-1100/1145)
( t=0.003mm )
16 A 1 kHz 1 mm/s 10 mm/m 1 success=0/5
18 A 2-3 success=0/5
19 A 2-3 Current Method
20 A 2-3 success=0/5
21 A 3-4 success=0/5
22 A 3-4 success=0/5
23 A 3-4 success=0/5
24 A 3-4 success=0/5
25 A 3 success=0/5
26 A 2-3 success=0/5
27 A 2 success=0/5
19 A 1 kHz 1 mm/s 6 mm/m 3-4 success=0/5
22 A 1 kHz 1 mm/s 5 mm/m 3-5 success=2/5
5 mm/m 3-5 success=3/5
6 mm/m 3-5 success=3/5, 15 min for 5 slits
7 mm/m 3-5 success=1/5
3 mm/s 6 mm/m 4-5 success=3/5
5 mm/s 3-4 success=0/6
10 mm/s 4-5 success=3/6
20 mm/s 4-5 success=2/6
40 mm/s 4-5 success=2/6
100 mm/s 4-5 success=3/6
10 kHz 1 mm/s 6 mm/m 1 success=0/5
40 kHz 1 success=0/5
24 A 1 kHz 1 mm/s 6 mm/m 4-5 success=1/5, but others are very easy to be dropped
8 mm/s 3-5 success=0/5
Black anodized
( t=0.003mm )
19 A 1 kHz 1 mm/s 5 mm/m 4 FLAMINGOS's mask
22 A 5 mm/m 4 success=1/5
24 A 5 mm/m 5 success=5/5 !!
7 mm/m 5 success=5/5 !!
10 mm/m 4 success=3/5
26 A 10 mm/m 2-3 success=0/4
Black painted
on usual mask
(alloy-1100/1145)
( t=0.003mm )
*
22 A 1 kHz 1 mm/s 6 mm/m 3-4 Black magic marker
success=1/5
Black coated
(alloy-1100/temp-O)
( t=0.002mm )
19 A 1 kHz 1 mm/s 5 mm/m 4 success=1/5
10 mm/m 4 success=3/5
22 A 5 mm/m success=5/5
10 mm/m 5 success=5/5 !!
4/8 outer slit cannot be cut
* Black coated = Coating for absorption of light by MacMaster. Anodized mask (top, back) Black coated mask (top, back) ------------------------------ Update memo ------------------------------ 10/10/2006 I tried to cut "black coated aluminum (t=0.002")" to make sure if the problem is reflection of laser beam (power loss). 10/6/2006 I could completely cut the black anodized mask for 1-time cutting(24A, feed=5-7mm/m). 10/5/2006 I cut a whole mask as the same science mask with best-cut settings(22A, feed=6mm/m). There seems to be many dull slits at outside of a mask. The same can be said always for other settings. 10/4/2006 I moved a left-lower hardstop for the laser and adjusted its position. Now both FOCAS's and MOIRCS's frames can be fit snugly. 10/3/2006 Somehow the laser work bench alignment is wrong. MOIRCS's cutting frame cannot fit the bench now. At the moment, I test parameters with FOCAS's frame.